Well I started this thread but then I got REALLY busy with work and personal life stuff. Just back around to checking it out. Developed about the way I thought it would.
This bit caught my eye.
...none of you guys were there, you may have experience and be top of your training class/best at your job, but none of you were there. you read the after reports and say, well it was an easy fix, airplane could have been saved. but you still werent there.
...but I'll apologize if you tell me that while flying that plane, the same malfunction happened, you identified it correctly and landed that plane.
semp
So here's a true tale of essentially the same situation that actually happened at my airline. This was late 80s IIRC.
There was a B737-200 off 17R at DFW going to ABQ, full passenger load. That day the right seater was PF. As soon as the gear unstuck, (there's that little 'click' when the landing gear solenoid unlocks) the stick shaker activated. The right seater kept flying as normal, normal pitch/normal power. In a 1/4 heart beat both the right seater's left hand and the Captain's right hand met momentarily the flap lever, confirming they were 20. In another quarter heart beat both pilot's hands then jumped to the throttles, confirming they were full forward. The right seater called out "we're doing 160, we ain't stalling". The Captain in the left seat said "keep flying". There was no configuration change at all. By this time the the FA's were dinging the hell out of the phone as the stick shaker was vibrating them in their tail seats and the Captain picked up the phone and calmed them down. The Captain noted it was his left side stick shaker motor that was activated. The Captain found and then pulled the left side AOA CB and there was instantly a return to normal flight operation and feel. The Captain then told the right seater to keep flying; he then coordinated a return to DFW. The right seater flew the entire pattern and landing. After parking an inspection was performed; the crew and mechanics looked at the left AOA at the gate. It was hanging by two wires. When the passenger service agent pulled the jetway away, the AOA vane got dinged.
This is essentially what happened to both the Lion Air and Ethiopian crews. The INITIAL problem was a plain vanilla AOA malfunction. The 737Max crews did not handle that malfunction correctly. The B737-200 crew did. It's just that simple.
So you have one highly experienced well trained crew THAT WAS THERE in essentially the same situation. They correctly identified it. In that case, after perhaps a minute, the situation was resolved with an easy fix and a normal landing was made.
Bottom line: FLY THE JET.