Originally posted by mw
JL165 trials
367 @ 3,200’ M.S., 397 @14,400’ F.S.
Of the performance obtained the report states:
“A further point of note is the full throttle height at + 18 lbs. of boost which is somewhat lower than has previously been obtained with Merlin 66 engines. A check of the air intake efficiency was taken during the tests, a minimum figure of 94% in level flight being shown at + 25 lbs. sq.inch boost pressure. It would seem therefore that the full throttle height of this engine is low.”
A low FTH will give poorer performace.
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Yep, too bad that even the new report on JL 165 did not show lower FTH than the others (save the experimental planes of course).
I guess there`s some wild consipracy going on, because we can see the JL 165 achieved FTH at 397 mph w. +18boost at 20 000 ft....

....and, for some odd reason, we also have the Merlin 66 power chart which actually shows that the FTH should be exactly at 20 000 feet at 400mph rammed speed.
In other words JL 165 reached exactly the FTH it should at +18lbs, ~20k ft. The "too low FTH" theory fails.

Furthermore, we see that JL 165 achieved ~14500 FTH at +25 lbs boost. Lookie again on the Merlin chart, the said FTH for +25lbs is again ~ 14 500 feet.
The "too low FTH" theory fails again. JL 165 reached exactly the same Full Throttle Heights in both MS and FS gear it should.
Apart from that, the whole case is pretty simple: Mike and Nashwan are so entitled to that the Spits should be superior to everything (but especially the 109), that they want to use performances measured on experimental machines.
Therefore they try, at every opportunity, discredit the JL 165 tests, despite the test notes it was a normal Spitfire in every aspect, with standard equipment, standard Merlin 66 engine, standard propellor, standard carburator and so on.
And so does, in view of this report, the "JL 165 was underperforming at +18lbs". Uh-oh, it did not.
The results from the other mid-1944 JL 165 report are ESTIMATES for +18lbs, worked out from +25lbs results. Previously MW and Nashwan claimed the JL 165 was "underperforming", pointing to these
estimated figures in comparison with results obtained with
experimental spitfires such as BS 543.
They believed the raise was far greater than actually, but this reports clearly points out the propellor could not take all the advanatage the increased power offered*, therefore their estimates for +18lbs understate the real speed of the aircraft.
*
" It should be noted that there is no increase in the absolute speed obtained by the increase of boost, and it would appear that the efficiency of the propeller is somewhat reduced at the higher rating. Originally posted by mw
In addition the condition with tropical filter is not representative of ADBG or ETO configuration.
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I guess Guppy can correct you on this, certainly it`s not hard to find filter equipped Spitfires in ETO, you know, the low mounted intake of the Spitty didn`t really like all the dust of Normandy`s provisional airfields.
“Won't figures for a Spit at 18 lbs do?” I would think so.
BS.543 or BS.310 might do.
Yep, both experimental planes with never-serialized equipment, ROFLOL. Perrrrfeeecct, - and typical Mike Williams.

Perhaps BS.543 would be better given its operational history: BS.543 was built as a Mk V, converted to Mk IX (Merlin 61) at Rolls Royce, Hucknall. First flight 22-10-42. Transferred to AFDU, Duxford 8-11-42; AAEE, Boscombe Down 13-12-42 with Merlin 66 installed; Vickers Armstrong 22-2-43; 403 Sqdn. 9-6-43; 611 Sqdn. 10-6-43; 485 Sqdn. 6-7-43. Failed to return from operations 22-8-43. BS.310 had the all-round better numbers on average though.
BS 543, Mr Williams means, the one with the never serialized Rotal XH54D-RM-S5 experimental airscrew.

Just as an aside, JL.165 ended up in North Africa which suggests they may have used 150 octane in the MTO. That's new on me.[/B]
Just like the rest of us, Mike, and we all wait in awe for your next flip flop making up the "150 grade Spitfires in ETO".
Like you did make up the +25lbs MkXIVs, which you know very well never existed in service, as their Griffon was derated to +21 lbs due to main bearing troubles.
